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To: Uncle Chip

It wouldn’t be the first time a pilot tried to go too high.

http://en.wikipedia.org/wiki/Pinnacle_Airlines_Flight_3701

The two pilots were exploring the performance limits of the empty CRJ-200 on the ferry flight. The pilots decided to test the limits of the CRJ, and join the “410 Club,” referring to pilots who pushed CRJs to their maximum approved altitude of Flight Level 410 (41,000 feet).

The accident sequence started when the pilots performed several non-standard maneuvers at 15,000 feet, including a pitch-up at 2.3g (23 m/s²) that induced a stall warning. They set the autopilot to climb at 500 ft/min to FL410. This exceeded the manufacturer’s recommended climb rate at altitudes above FL380. In the attempt to reach FL410, the plane was pulled up at over 1.2g, and the angle of attack became excessive to maintain climb rate in the thinner upper atmosphere. After reaching FL410, the plane was cruising at 150 knots (280 km/h), barely above stall speed, and had over-stressed the engines.

The anti-stall devices activated while they were at altitude, but the pilots overrode the automatic nose-down that would increase speed to prevent stall. After four overrides, both engines experienced flameout and shut down. The plane then stalled, and the pilots recovered from the stall at FL380 while still having no engines. At that altitude, there were six airports within reach for a forced landing. This led the pilots to pitch nose down in an attempt to restart the engines, which requires a dive sharp enough to attain the required 300 kt for a windmill restart to make the blades in the turbines windmill at 10% N2 (turbine rotational speed). The captain did not take the necessary steps to ensure that the first officer achieved the 300-knot or greater airspeed required for the windmill engine restart procedure and then did not demonstrate command authority by taking control of the airplane and accelerating it to at least 300 knots.

However, the turbine blades expanded contacting the honeycomb labyrinth seals allowing the metal to scrape on each other when the engine overheated with zero core rotation. When the engine is shutdown at altitude, the core begins to cool and the stator, including the static Interstage Static Seal (ISS), contracts at a faster rate than the adjacent rotating parts in both the radial and axial direction because of its faster thermal time constant. The relative rate of cooling of the stator and rotor results in an alignment of the rotating seal knife-edges aft of the normal operating groove in the static seal. If the clearances are tight enough and the relative cooling rates are right, contact can occur between the static and rotating seal elements. The resulting stiction can temporarily prevent the rotor from turning when only the force of ram air is applied to the core. Air Turbine Starter (ATS) torque has been shown adequate to overcome this restriction (NTSB Accident Information Brief Update for October 29, 2004.) Thus, when the engine cooled, the assembly did not match anymore and the blades could not rotate freely. The crew ended the descent when they had reached 230 kt but neither engine core (N2) ever indicated any rotation during the entire descent. Since they were too high for an APU start, the ram air turbine (known as an “Air Driven Generator” on Bombardier products) was deployed to power the aircraft, and the crew donned oxygen masks as the cabin slowly depressurized due to loss of pressurization air from the engines.


12 posted on 03/25/2014 7:33:35 PM PDT by Moonman62 (The US has become a government with a country, rather than a country with a government.)
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To: Moonman62

After 9-11, a friend’s wife refused to fly to her brother’s in Ireland or let their kids go with him, so he went himself. Yep, she was good with that.


24 posted on 03/25/2014 7:53:10 PM PDT by Insigne123 (It is the soldier, not the community organizer, who gives us freedom of the press)
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